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I successfully made a viable flex pcb on my second attempt. I started by printing the circuit onto a mailing envelope using my laser printer. Then I taped a piece of toner transfer paper for pcbs shiny side up directly over where the print on the envelope was. This way I could use just a tiny...
So armed with my successful electronic test of my prototype highside switch with driving circuit all passing, I determined now it is sufficiently validated to go through the process of converting it into a printable schematic and doing the whole DIY flat flex PCB making and acid etching process...
I just tested the positive high-side switch portion of the motor controller and everything seems to be working as intended. The section including all parts involved is circled in a bold blue line to indicate the portion I just tested successfully. One issue I'm having though is that the drain...
Here's the thermal tape I bought for mosfet heat sinking off Amazon:
Okay so here I have attached the LED and resistor pair with their 30ga wire wrapping wire onto my highside mosfet's front face. I may add conductive silver paste to the wire wraps in the future if any issues come up there. However, I am wondering if just tightly wrapping it in electrical tape...
Couple updates: An audience member redid my brushless DC motor schematic in the traditional commonplace formatting which for most is easier/quicker to read and understand due to familiarity. So I'm reposting it. It looks mostly accurate although I have since added a 100nF ceramic capacitor...
Ok so I decided to use 30 gauge wire wrapping wire and wire wrap that onto my nickel strips that I connected onto my LED setup then trim off any excess nickel strip. What I like about this is this wire is very fine so it takes up hardly any space and by being able to wrap it on I did not have to...
Well I finally got back to the electronics after about a month long detour real life interruption. All kinds of stuff slowed my progress on this session. But I got stuff done nonetheless. 0603 LED to 0805 resistor and some nickel strip leads coming off. Tested and working. This will be the...
I started some testing on some subsections of the BLDC motor controller and ran into some problems and learned several things. I'm working with chatgpt to resolve each issue and have been updating my schematic to reflect alot of the changes I am making. One thing I learned is that for the high...
Back on the electronics again. Have been going over my BLDC motor schematic and making some little tweaks to it. Here's the updated schematic. It's a combination of lots of other schematics I've found online as well as some chatgpt help. With 1 being no clue and 10 being absolute expert tier in...
I installed two tensioners for the robot and they were seriously successful overall in testing. So much so that I am now confident enough in the entire pulley system to move onto the custom mini BLDC motor controller to get the motor to run motorized tests of finger movements next. Well after a...
Okay so the bracelet cord self untied quickly so I'm going back to my previous approach of tying off both ends of the bracelet cord with a fishing crimp sleeve. While trying to cut in half fishing crimp sleeves with my mini miter saw I noticed it was a difficult process and not ideal. So I came...
Ok I figured out a bit easier way: tie a knot at each end of the strip of bracelet cord and then tie my nylon thread off onto the bracelet cord inside that bracelet cord knot. The bracelet cord knot on each end acts as an endstop. Seems to work great so far and cuts down on materials this way...
I figured out a robust way to make the extension cord for finger extension using the bracelet cord and a fishing crimp sleeve. The idea is to crimp the two ends of a folded in half strip of bracelet cord and this way both ends can be sewn down into the fabric without any gluing which could...
So in recent testing a fresh issue I ran into was the TPFE tubing would start gradually pulling through its tightly wrapped tape sleeve to my surprise. Its low friction surface gradually pulls free of the tape over time. To resolve this, I decided to thread through the tip of the tubing to...
The tension spring mounted to the motor setup upon further testing seems like a somewhat bad method. The issue I'm having is too much play in the tubing running between that spring and the finger joint. When tension is applied to that spring by way of the tubing, the tubing recoils and moves...
I finally finished making the tensioner mechanism for the winch in place pulley and I taped it off up the string descending from the ceiling and taped the far end of it onto the ceiling. I noticed I have to keep it as straight as possible since when curling with too much turning the elastic...
Minor update: I have now carefully mounted the PTFE tubing that leads to the elastic string tensioner for the winch in place pulley. I mounted it snugly to the side of the PTFE tubing coming off the same winch in place pulley that leads to the Archimedes pulley system. I routed both of these...
Sometimes to get the braided PE fishing line threaded through the fine PTFE tubing can be tricky, so I came up with a neat device to assist in this. I will be making a threading tool based on a needle threader tool I've been using. It's basically a wire folded in half that you shove through a...
Ok so I currently have an order for 0.2x1x1000mm tension springs stuck in customs for weeks and placed another order just today for the same in hopes it goes through faster. But at $9 for a single spring that is 3ft long, I am feeling RIPPED OFF on price. It is bullcrap. All relating to the...
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